FUJI错误代码查询 - 第1090页

3,CP5,CP6,CP6M,CP65,CP642,CP643,GL5,GL541,GSP5,GP2,GP3,GP551,GP6,IP3 Cause: Too much time elapsed waiting for the board to be received on the in conveyor. The board may have been removed. (I/O 1:ON, 2:OFF, 3:OFF) The in-…

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the cancel stopper sensor.
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Code: 15010204
Display: Conv. PLC Alarm: MCID
PCB Transport Error:MCID
Deceleration sensor
does not turn on
Used by: CP5,GSP5,GP2,GP3,GP551,GP6,IP3,CP643
Cause:
Remedy:
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Code: 15010301
Display: PCB Transport Error: IN-A
Used by: CP5,GSP5,GP2,GP3,GP551,GP6,IP3
Cause: The time required to transport the board between each conveyor exceeded the preset limit. The
appropriate setting is made (1:ON 2:OFF 3:OFF). Three seconds after the deceleration point is activated
the board start point is not on, an alarm occurs and the machine is stopped.
Remedy: Check that there is no board stuck between this point and the previous production stage.
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Code: 15010302
Display: PCB Stopper Error: IN-A
Used by: CP5,GSP5,GP2,GP3,GP551,GP6,IP3
Cause: Stopper alarm. (1:OFF 2:ON 3:OFF) The stopper between each conveyor produced a cycle alarm.
This occurs when the time setting between the leading edge and the leaving edge is not on. After the
stopper moves vertically, the stopper vertical movement check sensor does not activate within 5 seconds to
check the position of the board stopper.
Remedy: Check for obstacles hindering stopper movement. If these obstacles (such as a board) exist,
remove them. If there are no obstacles, check the movement of the stopper at the I/O display, and check
the cancel stopper sensor.
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Code: 15010303
Display: Command Error: IN-A
Used by: CP5,GSP5,GP2,GP3,GP551,GP6,IP3
Cause: The operator has attempted to unload or change boards when there is no board. The operator
has attempted to load a board when there is already a board. If there was a board on the conveyor the
machine attempted to load the board. If there was no board, the machine attempted to clear off the board.
Remedy: Use the correct command based on conditions. Check that the command you are using can be
carried out under current conditions. Also, check the conveyor board arrival confirmation sensor at the
I/O dsiplay.
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Code: 15010304
Display: Conv. PLC Alarm: IN-A.
Used by: CP5,GSP5,GP2,GP3,GP551,GP6,IP3
Cause: The CPU module (board loader PLC) is not operating normally. The user cannot set this.
Remedy: Contact Fuji.
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Code: 15010401
Display: PCB Transport Error: IN
PCB Transport Error:I_LIFT
Chk brd conveyance at I-lif
Used by: CP4-1,CP4-2,CP4-
第 1089 页
3,CP5,CP6,CP6M,CP65,CP642,CP643,GL5,GL541,GSP5,GP2,GP3,GP551,GP6,IP3
Cause: Too much time elapsed waiting for the board to be received on the in conveyor. The board may
have been removed. (I/O 1:ON, 2:OFF, 3:OFF)
The in-conveyor failed to convey a board (or boards) correctly.
Remedy: Check that the board has not become stuck on the conveyor.
Check the in-conveyor width.
Make sure the in-conveyor board sensors (the I/O input signals listed below) correctly detect the presence
of boards on the conveyor. The board gap sensor should be ON when there is no boards,and OFF when a
board is present.
I/O input signals(CP643):
LX003: IN1 board deceleration start point sensor
LX004: IN1 board arrival sensor
LX007: IN1/IN2 board gap sensor
LX008: IN2 board deceleration start point sensor
LX009: IN2 board arrival sensor
LX017: IN-conveyor board load sensor
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Code: 15010402
Display: PCB Stopper Error : IN
PCB Stopper Error:I_LIFT
Check board-stopper up/down sensors on the I_LIFT
Used by: CP4-1,CP4-2,CP4-
3,CP5,CP6,CP6M,CP65,CP643,GL5,GL541,GSP5,GP2,GP3,GP551,GP6,IP3,NXTP
Cause: Stopper alarm (I/O 1:OFF, 2:ON, 3:OFF). This is a stopper cycle alarm for the stopper between
each conveyor. This error includes the cases where the sensor is not on for the regulated time during
engagement or disengagement. The sensor that checks that the stopper has moved up (disengaged) or
down (engaged) 5 seconds after it moves up or down does not work.
The in-conveyor mid-stopper engaged,but the engaged limit sensor did not turn ON within the specified
time.
The in-conveyor mid-stopper disengaged,but the disengaged limit sensor did not turn ON within the
specified time.
The in-conveyor mid-stopper engaged and disengaged limit sensors both ON.
Remedy: Check the conditions under which the stopper moves. If there is an interfering object (like a
board), remove it. If there is no interfering object, use the I/O to check the stopper engagement and
disengagement sensor.
Make sure the in-conveyor mid-stopper engages and disengages smoothly.
Make sure the engaged and disengaged limit sensors have been attached at the correct positions.
Make sure the engaged and disengagedlimit sensors (the I/O input signals listed
below) turn ON and OFF.
Make sure the engaged and disengagedlimit sensors (the I/O input signals listed
below) turn ON and OFF correctly when the in-conveyor mid-stopper is engaged and disengaged.
I/O input signals(CP643):
LX005: IN-conveyor mid-stopper engaged(up) limit sensor
LX006: IN-conveyor mid-stopper disengaged(down) limit sensor
<img src="$LKEY_ERRIMG_MC$/15010402.PNG">
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Code: 15010403
Display: Command Error : IN
PCB Setting Error:I_LIFT
Chk brd status on in-lifter
Used by: CP5,CP6,CP6M,CP65,CP642,CP643,GSP5,GP2,GP3,GP551,GP6,IP3
第 1090 页
Cause: A board unload or a change command was sent when there was no board. If there is a board on
the conveyor, an attempt was made to load the board. If there is no board on the conveyor, an attempt
was made to unload the board.
Two boards are present even though single board production is in effect.
Two boards are present even though a single board feed instruction was issued during double board
production.
The in-conveyor cannot convey boards due to poor board positioning.
The status of boards in the in-conveyor cannot be checked.
Remedy: Input the correct command. Check the conveyor conditions. and check that the command can
in fact be carried out. Otherwise, use the I/O to check that the board arrived sensor on the conveyor is
operational.
Set boards in the in-conveyor so that the quantity of boards is appropriate to the production method in
effect.
Set boards in the correct positions.
Make sure the in-conveyor board sensors (the I/O input signals listed below) correctly detect the presence
of boards in the conveyor. The board gap sensor should be ON when there is no board,and OFF when a
board is present.
I/O input signals(CP643):
LX003: IN1 board deceleration start point sensor
LX004: IN1 board arrival sensor
LX007: IN1/IN2 board gap sensor
LX008: IN2 board deceleration start point sensor
LX009: IN2 board arrival sensor
LX017: IN-conveyor board load sensor
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Code: 15010404
Display: Conv. PLC Alarm : IN
Board check error:I_LIFT
Should be no brd on in-lift Chk brd status
Used by: CP5,CP642,CP643,GSP5,GP2,GP3,GP551,GP6,IP3
Cause: The CPU module (board loader PLC) is not working properly.
The in-lifter board sensors are abnormal. ( For example,a sensor is ON
even though it should be OFF.
Remedy: Contact Fuji.
Make sure the in-conveyor board sensors (the I/O input signals listed below) tuen ON and OFF correctly.
The board gap sensor should be ON when there is no board,and OFF when a board is present.
I/O input signals(CP643):
LX003: IN1 board deceleration start point sensor
LX004: IN1 board arrival sensor
LX007: IN1/IN2 board gap sensor
LX008: IN2 board deceleration start point sensor
LX009: IN2 board arrival sensor
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Code: 15010405
Display: Cylinder cycle alarm:I_LIFT
Up/down movement of the I_LIFT time up
Used by: CP643
Cause: The in-lifter was raised,but the upper limit sensor did not turn ON within the specified time.
The in-lifter was lowered,but the lower limit sensor did not turn ON within the
specified time.
The in-lifter upper and lower limit sensors are both ON.
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