Error Code List.pdf - 第48页
RL1 31 ERROR CODE LIST 2.4 Errors DA8EEC- 91-210- A0 2.4- 25 2209 Rail down condit ion not sa tisfies ( left rail retu r n l imit ) DESCRI PTIO N Rail down act i on was not done, because of the l ack o f the ra il down c…

RL131
ERROR CODE LIST
2.4 Errors
DA8EEC-91-210-A0
2.4-24
1920
Feeder install error
DESCRIPTION
The feeder installation is abnormal.
CAUSE
The feeders may not have been installed properly.
SOLUTION
Check the installation condition of the feeders.
NOTE
2003
PCB carry in restart cancel (right rail belt)
DESCRIPTION
The restart of the PCB carrying in was canceled.
CAUSE
When the carrying in operation was restarted by the safety stop release, PCB was detected at the right rail exit.
SOLUTION
Please restart the operation after confirming PCB on a right rail.
NOTE
2011
PCB carry in restart cancel (right rail exit)
DESCRIPTION
The restart of the PCB carrying in was canceled.
CAUSE
When the carrying in operation was restarted by the safety stop release, PCB was detected at the right rail exit.
SOLUTION
Please restart the operation after confirming PCB on a right rail.
NOTE
2012
PCB carry in restart cancel (right rail exit)
DESCRIPTION
The restart of the PCB carrying in was canceled.
CAUSE
When the carrying in operation was restarted by the safety stop release, PCB was detected at the right rail exit.
SOLUTION
Please restart the operation after confirming PCB on a right rail.
NOTE
2052
PCB carry out restart cancel (left rail belt)
DESCRIPTION
The restart of the PCB carrying out was canceled.
CAUSE
When the carrying out operation was restarted by the safety stop release, PCB was detected at the left rail exit.
SOLUTION
Please restart the operation after confirming PCB on a left rail.
NOTE
2079
PCB carry out restart cancel (left rail exit)
DESCRIPTION
The restart of the PCB carrying out was canceled.
CAUSE
When the carrying out operation was restarted by the safety stop release, PCB was detected at the left rail exit.
SOLUTION
Please restart the operation after confirming PCB on a left rail.
NOTE

RL131
ERROR CODE LIST
2.4 Errors
DA8EEC-91-210-A0
2.4-25
2209
Rail down condition not satisfies (left rail return limit)
DESCRIPTION
Rail down action was not done, because of the lack of the rail down condition.
CAUSE
Left rail return limit has been turned off.
SOLUTION
It is necessary to have turned on the left rail return limit to down rail.
NOTE
2216
Rail down condition not satisfies (positioner lever return limit)
DESCRIPTION
Rail down action was not done, because of the lack of the rail down condition.
CAUSE
Positioner lever return limit has been turned off.
SOLUTION
It is necessary to have turned on the positioner lever return limit to down rail.
NOTE
2221
Rail down condition not satisfies (right rail return limit)
DESCRIPTION
Rail down action was not done, because of the lack of the rail down condition.
CAUSE
Right rail return limit has been turned off.
SOLUTION
It is necessary to have turned on the right rail return limit to down rail.
NOTE
2223
Rail down condition not satisfies (servo switch)
DESCRIPTION
Rail down action was not done, because of the lack of the rail down condition.
CAUSE
Servo switch has been turned off.
SOLUTION
It is necessary to have turned on the servo switch to down rail.
NOTE
2225
Rail down condition not satisfies (transfer arm return limit)
DESCRIPTION
Rail down action was not done, because of the lack of the rail down condition.
CAUSE
Transfer arm return limit has been turned off.
SOLUTION
It is necessary to have turned on the transfer arm return limit to down rail.
NOTE
2231
Rail down condition not satisfies (XY origin)
DESCRIPTION
Rail down action was not done, because of the lack of the rail down condition.
CAUSE
X or Y axis origin sensor has been turned off.
SOLUTION
It is necessary to have turned on the X and Y axis origin sensor to down rail.
NOTE

RL131
ERROR CODE LIST
2.4 Errors
DA8EEC-91-210-A0
2.4-26
2232
Rail down condition not satisfies (XY movement)
DESCRIPTION
Rail down action was not done, because of the lack of the rail down condition.
CAUSE
X or Y axis is moving
SOLUTION
It is necessary to have stopped X and Y axis to down rail.
NOTE
2258
Arm carry condition not satisfies (left rail traverse limit)
DESCRIPTION
Transfer arm movement was not done, because of the lack of the transfer arm movement condition.
CAUSE
Left rail traverse limit has been turned off.
SOLUTION
It is necessary to have turned on the left rail traverse limit to move transfer arm.
NOTE
2270
Arm carry condition not satisfies (right rail traverse limit)
DESCRIPTION
Transfer arm movement was not done, because of the lack of the transfer arm movement condition.
CAUSE
Right rail traverse limit has been turned off.
SOLUTION
It is necessary to have turned on the right rail traverse limit to move transfer arm.
NOTE
2273
Arm carry condition not satisfies (servo switch)
DESCRIPTION
Transfer arm movement was not done, because of the lack of the transfer arm movement condition.
CAUSE
Servo switch has been turned off.
SOLUTION
It is necessary to have turned on the servo switch to move transfer arm.
NOTE
2275
Arm carry condition not satisfies (transfer arm return limit)
DESCRIPTION
Transfer arm movement was not done because of the lack of the transfer arm movement condition.
CAUSE
Transfer arm return limit has been turned off.
SOLUTION
It is necessary to have turned on the transfer arm return limit to move transfer arm.
NOTE
2281
Arm carry condition not satisfies (XY origin)
DESCRIPTION
Transfer arm movement was not done because of the lack of the transfer arm movement condition.
CAUSE
X or Y axis origin sensor has been turned off.
SOLUTION
It is necessary to have turned on the X and Y axis origin sensor to move transfer arm.
NOTE