ERR-LIST-ACM - 第10页

555 Transport :\tunexpected board in run-out An unexpected board was detected at the second sensor in the run-out. - Unexpected board at second sensor in the run-out - Defective sensor (either first or second run-out sen…

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547 Transport :\twrong flash ID Flash PROM is write protected.
- The flash prom on the controller is of the wrong type.
- No jumper X44 is installed on the controller card.
- Replace with correct type: 28F256 (Intel 89B9 or SGS 20AA).
- Install jumper X44 on the controller card.
548
Transport :\tUnexpected board at
run-in
The first sensor in the run-in
detects an unexpected board.
- Unexpected board at first sensor.
- Defective first sensor.
- Malfunction in sensor communication.
- Remove the board from the run-in.
- Check the first sensor of the run-in.
- Retry operation and continue, if not correct contact your service
representative.
549
Transport :\tUnexpected board in
run-in
An unexpected board was
detected at the second sensor of
the run-in.
- Unexpected board at second sensor in the run-in.
- Defective sensor (either first or second run-in sensor).
- Malfunction in sensor communication.
- Remove unexpected board from run-in.
- Check first and second sensor of the run-in.
- Retry operation and continue, if not correct contact your service
representative.
550
Transport :\tUnexpected board in
work-area
An unexpected board was
detected on the first sensor in the
work-area
- Unexpected board at first sensor in the work-area.
- Defective sensor (either first or second work-area sensor).
- Malfunction in sensor communication.
- Remove unexpected board from work-area.
- Check first and second sensor in work-area.
- Retry the operation and continue, if not correct contact your service
representative.
551
Transport :\tUnexpected board in
work-area
An unexpected board was
detected on the second sensor in
the work-area
- Unexpected board at second sensor in the work-area
- Defective sensor (either first or second work-area sensor).
- Malfunction in sensor communication.
- If none of above, possible reflection on the XY-robot.
- Remove unexpected board from the work-area.
- Check first and second sensor in the work-area.
- In case of reflection, decrease the sensitivity of that sensor sligthly. Be sure
the sensitivity is right to detect all kinds of boards, which have to be p
552
Transport :\tUnexpected board in
work-area
An unexpected board was
detected at the third sensor in the
work-area.
- Unexpected board detected in the work-area.
- Defective sensor (either second or third work-area sensor).
- Malfunction in sensor communication.
- Remove unexpected board from work-area.
- Check second and third sensor in work-area.
- Retry the operation and continue, if not correct contact your service
representative.
553
Transport :\tUnable to position
board in work area
The transport is not able to
position a board on the second
sensor in the work-area.
- Transport speed is too large.
- Acceleration is too low.
- Reduce board transfer speed.
- Enlarge the belt acceleration.
554
Transport :\tunexpected board in
run-out
The first sensor in the run-out
detects an unexpected board
- Unexpected board at first sensor.
- Defective first sensor.
- Malfunction in sensor communication.
- Remove unexpected board from run-out.
- Check the first sensor of the run-out.
- Retry operation and continue, if not correct contact your service
representative.
555
Transport :\tunexpected board in
run-out
An unexpected board was
detected at the second sensor in
the run-out.
- Unexpected board at second sensor in the run-out
- Defective sensor (either first or second run-out sensor).
- Malfunction in sensor communication.
- Remove unexpected board from the run-out.
- Check first and second sensor of the run-out.
- Retry the operation and continue, if not correct contact your service
representative.
556
Transport :\tMissing board in run-
in
The previous machine signaled
the arrival of a board. However,
the board was not detected within
the time frame
on the first sensor in the run-in
section.
- The board is stuck between the previous machine and the run-
in.
- Defective sensor (first run-in sensor).
- The first sensor is not correctly adjusted.
- Defective wiring I/O.
- Remove the stuck board.
- Adjust the transport width to match the board dimensions.
- Adjust the preceding machine so that it is correctly in line.
- Retry the action.
557
Transport :\tMissing board in run-
in
A board was detected at the first
sensor in the run-in. However, the
board was not detected within the
time frame
on the second sensor in the run-in
section.
- The board is stuck between the first and second sensor of the
run-in.
- Defective sensor (second run-in sensor).
- The second sensor is not correctly adjusted.
- Defective wiring I/O.
- Check width of the transport system, if necessary adjust the width.
- Retry the operation and continue.
- Check the second sensor in the run-in.
- Check wiring I/O.
- Check if sensor sesitivity is set to maximum.
558
Transport :\tMissing board in work-
area
A request was made to transport a
board from the run-in to work-
area. The transport was started,
however, the board was not
detected within the time frame on
the first sensor in the work-area
section.
- The board is stuck between the run-in and the first sensor of
the work-area.
- Defective sensor (first sensor of the work-area).
- The first sensor is not correctly adjusted.
- Defective wiring I/O.
- Check the width of the transport system, if necessary adjust the width.
- Retry the operation and continue.
- Check the first sensor in the work-area.
- Check wiring I/O.
- Check sensor adjustment.
559
Transport :\tMissing board in work-
area
A board was detected at the first
sensor in the work-area. However,
the board was not detected within
the time frame
on the second sensor in the work-
area section. Or the transport was
not able to transport the board out
of the work-area.
- The board is stuck between the first and second sensor of the
work-area.
- Defective sensor (second sensor in the work-area).
- The second sensor is not correctly adjusted.
- Defective wiring I/O.
- Check the width of the transport system, if necessary adjust the width.
- Retry the operation and continue.
- Check the second sensor in the work-area.
- Check wiring I/O.
- Check sensor adjustment.
560
Transport :\tMissing board in work-
area
A board was detected at the
second sensor in the work-area.
However, the board was not
detected within the time frame
on the third sensor in the work-
area section. Or the transport was
not able to transport the board out
of the work-area.
- The board is stuck between the second and third sensor of
the work-area.
- Defective sensor (third sensor in work-area).
- The third sensor is not correctly adjusted.
- Defective wiring I/O.
- Check the width of the transport system, if necessary adjust the width.
- Retry the operation and continue.
- Check the third sensor in the work-area.
- Check wiring I/O.
- Check sensor adjustment.
561
Transport :\ttime-out occurred on
board move
This message is obsolete and
should not occur. - Report error to your service representative.
562
Transport :\tMissing board in run-
out.
A request was made to move a
board out the work-area. The
movement was started but the
board was not detected within the
time frame on the first sensor in
the run-out section.
- Board stuck between work-area and run-out.
- Defective sensor (first sensor in run-out).
- The first sensor in the run-out is not correctly adjusted.
- Defective wiring I/O.
- First sensor in run-out not correctly adjusted.
- Check the width of the transport system ,if necessary adjust the width.
- Retry the operation and continue.
- Check the first sensor in the run-out.
- Check wiring I/O.
- Check sensor adjustment.
563
Transport :\tMissing board at run-
out stop sensor.
A board was detected at the first
sensor in the run-out. However,
the board was not detected within
the time frame
on the second sensor in the run-
out section.
- Board stuck between first and second sensor of run-out.
- Defective sensor (second sensor in run-out).
- The second sensor in the run-out is not correctly adjusted.
- Defective wiring I/O.
- Second sensor in run-out not correctly adjusted.
- Check the width of the transport system ,if necessary adjust the width.
- Retry the operation and continue.
- Check the second sensor in the run-out.
- Check wiring I/O.
- Check sensor adjustment.
564
Transport :\tPrevious board did not
leave work-area
The transport was not able to
position a board in the work-area
because the previous board did
not leave the work-area in time.
- Board stuck between work-area and run-out.
- Sensor malfunction.
- Board is larger as specified in action spec.
- Remove the board for work-area.
- Adjust action spec.
565
Transport :\tUnable to position
board in work-area
The transport is not able to
position a board on the second
sensor in the work-area.
- Transport speed is too large.
- Acceleration is too low.
- reduce board transfer speed.
- enlarge the belt acceleration.
566
Transport :\tIllegal state to execute
command (%1)
Command refused because the
transport controller firmware is in a
wrong state. Software error.
- Retry and continue.
- Restart the system.
- Report error to your service representative.
567
Transport : Transport width out of
range (command: %1)
The requested function cannot be
executed because one or more
parameters (e.g. transport width)
are invalid.
- Coplanarity checker, Flux unit or Wafer handler has been
configured;
maximum transport width when Coplanarity checker
configured: 406mm.
maximum transport width when Flux unit configured: 350
mm.
maximum transport width when W
- Check transport width and modify when necessary.
- Retry and continue.
- Restart the system.
568
Transport :\tCommand (%1) is
refushed
A message is refushed by the
transport controller.
- A command was given to the transport while the same
command was already executing. This might appear when a
transport jogging is in progress.
- Software error.
- Retry the operation.
- Report error to your service representative.
569
Transport :\tTime-out occurred
while executing command (%1)
A transport command is not
finished within a fixed time frame.
- Transport speed is too low.
- Hardware failure.
- Software error.
- Retry the operation.
- Report error to your service representative.
570 Unable to start the transport
The system was not able to start
the transport.
- No servo power present.
- Transport hardware failure. - Switch on servo power.
571
Transport :\trecovery failed, please
check transport
This message is obsolete and
should not occur. - Report error to your service representative.