ERR-LIST-ACM - 第4页

216 Head : %1\x0ASection : %2\x0AFeeder : %3\x0AChannel : %4\x0AComponent : %5\x0A 217 Section : %1\x0AFeeder : %2\x0AChannel : %3\x0AToolbit : %4\x0ANozzle : %5\x0AVacuum specified : %6\x0AVacuum measured : %7\x0ACompon…

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202
Fail to start transport for error
recovery
An attempt to start the transport
during an error recovery action
failed. - No servo power present. - Switch on servo power.
203 Unknown warning The warning is not specified yet. - Report error to your service representative.
204
Unknown error reported by the
system The error is not defined yet.
- An error was detected which is unknown to the human
interface.
- Retry and continue.
- Report error to your service representative.
205 %1 :\tUnknown warning The warning is not defined yet.
- A warning was detected which is unknown to the human
interface.
- Retry and continue.
- Report warning to your service representative.
206 Undefined process error
The process error is not defined
yet.
- Retry and continue.
- Report error to your service representative.
207 Retry action failed The retry action is unsuccessful. - A machine or process error occurs during the retry action.
- Check error cause and solve error.
- Retry and continue.
- If the retry action still fails, restart the system and report error to your service
representative.
208 Error reason unknown
The process controller signalized
errors, but no errors where
reported, so the reason of the
error is unknown.
- Continue
- Report error to your service representative.
209
Requested function can not be
executed.
The requested function
(Calibration) can not be executed
in this machine state.
- A board is present in the machine.
- An error is not solved on the machine
- Solve error (skip board).
- Remove board out of machine (skip board or using run-out function).
210
Sorry, this function (%1) has not
been implemented (yet)
A function was activated that has
not been implemented in the
current software version.
- Functions that are not complete yet, should not be accessible
for the user.
- By mistake, this function is reachable for the user.
- Clear the error, and do not use the function again, you should not be needing
it.
- Report error to your service representative.
211
System communication error on:
%1
An unexpected system error
occurred.
- Retry and continue.
- Restart the system.
- Report error to your service representative.
212 Communication failure in system
A communication error has been
occurred between the system
controller and the process
controller.
- No connection between the two systems.
- Malfunctioning network card on either system.
- A software problem in the machine.
- Check the coax cable connection between the two systems.
- Check the proper working of the network cards (using diagnostic software).
- Restart the system.
- Report error to your service representative.
213
Single step during error recovery
finished, press retry to resume
The machine is in step mode an
has finished a single step during
the retry of an error. - Press retry again to proceed with the next step in recovering the error.
214 Machine failure An unexpected situation occurred.
- Make a logdisk as described in the Service Manual.
- Restart the system.
- Report error to your service representative.
215
No extra information available
216
Head : %1\x0ASection :
%2\x0AFeeder : %3\x0AChannel :
%4\x0AComponent : %5\x0A
217
Section : %1\x0AFeeder :
%2\x0AChannel : %3\x0AToolbit :
%4\x0ANozzle : %5\x0AVacuum
specified : %6\x0AVacuum
measured : %7\x0AComponent :
%8
218
Automatic temperature drift
calibration failed
The automatic temperature drift
calibration failed. - Retry the operation.
219
Automatic feedersection
calibration failed
The automatic feedersection
calibration failed. - Retry the operation.
300 Machine is not stopped
The requested machine action is
only possible if the machine is
stopped.
- The requested machine action is only possible if the machine
is stopped. - Stop the machine.
301
Machine can not be started while
errors are pending
Production of boards cannot
proceed when machine errors are
pending. - Machine errors are pending. - Solve (retry) all errors and try action again.
302 No order available
The machine can not be started if
there is no default or selectable
order. - There is no order available. - Create an order with the correct selection state and try again.
303
Process errors occurred during
machine start-up
During machine start-up process
errors were detected, causing the
machine to stop.
- Please refer to the error-recovery dialog in the production menu for
appropriate actions.
304 A default order exist.
The production mode of the
machine can not be switched to
pass-through mode. - A order exists in the order schedule. - Abort the current order and try again.
305
The machine contains a
suspected or skipped board
The machine contains a
suspected or skipped board.
- Depending on whether or not the board must be removed from the machine,
the board can be removed. Then perform a retry.
306
Unable to execute production
command - A similar production command is currently being executed - Wait till the current command is executed and then try again
307
Unable to execute passthrough
command - A similar command is currently being executed - Wait till the current command is executed and then try again
400 Action spec download failed
A communication error has been
occurred between the system
controller and the process
controller.
- No connection between the two systems.
- Malfunctioning network card on either system.
- A software problem in the machine.
- Check the coax cable connection between the two systems.
- Check the proper working of the network cards (using diagnostic software).
- Make a logdisk as described in the Service Manual.
- Select skip board in error window.
- Restart the system.
-
401 Setup check failed
The feeder, transport and/or head
setup is not verified or differs from
the previous used setup.
- The feeder setup must be verified. The used setup differs
from the previously used (No family or other family).
- The transport setup is checked by the system; the currently
used setup may differ.
- The toolbit setup is checked by the system, the curr
- Use skip action if you are sure that the setup is correct, otherwise verify the
setup.
402
Order not started, still machine
errors pending or some modules
not calibrated
- The process controller state
needed to download an action
specification is not reached.
- Machine errors are pending.
- One or more modules are not calibrated.
- Retry action.
- Calibrate the not calibrated modules.
- Restart the system.
403 Action spec download failed System failure.
- Corrupted file system.
- Illegal update has been occurred. - Contactl your service representative.
501 Transport :\tposition error lift
The servo system of the transport
lift is not able to move to the
requested position, or the servo
system has detected a position
failure, which exceeds the error
limit.
- The requested position is outside the mechanical range.
- The friction of the lift mechanics is too high.
- The servo system is defective. - Maintenance is required in case of a friction problem.
502 Transport :\ttracking warning lift.
The lift servo system has detected
a position failure, which exceeds
the warning limit.
- The friction of the lift mechanics is increasing; maintenance
may be required. - Maintenance is required.
503 Transport :\tLift not calibrated
An attempt was made to move the
lift while the lift was not calibrated.
- The transportsystem was not calibrated.
- Defective transport controller.
- Calibrate the lift.
- If error still occurs, replace transport controller.
504
Transport :\tcommunication time-
out lift.
The servo system of the transport
lift reacts too slow. - Hardware error on transport controller.
- Retry and continue.
- Restart the system
- Contact your service representative.
505
Transport :\tCommunication error
lift
Communication error occurred
inside the transport controller.
- Wrong parameters sent to servo controller; this error should
not occur.
- Retry and continue.
- Restart the system
- Report error to your service representative.
506
Transport :\tZero coarse not found
at homing lif.
During lift homing the zero coarse
sensor (EPD) could not be
located.
- EPD is defective.
- EPD wiring malfunction.
- Lift hardware failure.
- Retry and continue.
- Restart the system
- Contact your service representative.
507
Transport :\tZero fine not found at
homing lif.
During lift homing the zero fine
index on the encoder could not be
located. - Lift hardware failure.
- Retry and continue.
- Restart the system
- Contact your service representative.
509 Transport :\tposition error run-out
The servo system of the transport
run-out is not able to move to the
requested position
- Run-out belt jammed.
- The friction of the run-out mechanics is too high
- The servo system is defect.
- Check run-out mechanics for being jammed.
- Maintenance or repair is required.
- Contact your service representative.
510
Transport :\ttracking warning run-
out
The run-out servo system has
detected a position failure.
- The friction of the run-out mechanics is increasing;
maintenance may be required. - Maintenance is required.