00198500-02_VD_711.1_R18-1_DE_EN - 第30页
Station Software 71 1.1 (R18 - 1) / Versio n Description 05/2018 Edition 30 D1 - 147192301 The grouping of MTC/WPC component s d id not work. D1 - 147324601 The firmware downl oad onto a new WPC 6 failed 2 times with a c…

Station Software 711.1 (R18-1) / Version Description 05/2018 Edition
29
D1-140734101 Head cycle counts in the SIPLACE Pro optimized results and in the actual
machine run did not match each other.
D1-140943701 The images for the feeder pickup position were not put together correctly..
D1-141418801 Conveyor sub-system 1: 30450 Unspecified hardware error.
D1-142534201 Board barcodes had to be programmed with 2 mm offset on an SX V2
placement machine. The original data did not work.
D1-144465801 Endurance run functions could not be selected in the Manual Operations; an
error message was displayed immediately.
D18275-3701 TX2i placement machine: Machine stopped during normal production without
any error message.
Table 9-2: Corrected errors station software version 711.0
710.1 SP1
Error No.
Error description
D1-141115401
eSW: a board in the input conveyor was not transported into the placement
area.
D1-145118902 Production did not start after confirming nozzle configuration.
D1-145571745
D1-147043656
D1-145527801
eSW: the z axis was not able to initialize during the reference run; the
following error handling let the segment drop out of the raceway.
D1-146272909
After a restart the language was set to English although it was German
before.
D1-146361597 The "feed forward" button was not active.
D1-146433623
LED Centering: the machine omitted the validation of the glass plate before
placing the led on it.
D1-146449111
D1-146429348
The automatic calibration of the Vacuum Tooling failed because of incorrect
positions for chuck fiducials.
D1-146494912
SIPLACE ProgressData event "ProductionProgress" delivered wrong Context-
ID (CtxId).
D1-146524401
After program download a board was placed although one pin was declared
as faulty.
D1-146590633
eSW: there was a transport error when a special carrier was used because
the board sensor in the output section was activated too early.
D1-146802617
eSW: If the upstream machine was stopped and the conveyor software tried
to exchange a board in processing area 1, the board in the input area could
not be moved until the upstream machine was started.
D1-146821856 Conveyor: the width adjustment could not adjust the maximum width.
D1-146933102
D1-146935404
When BETZ feeders were used, there were more pickup errors with segment
1 (CPP head) than with the other segments.
D1-147134301 Gantry 2 stopped over the WPC6 tray without error message.
D1-147150443 The "automatic check of nozzle changer" function did not work.
D1-147177501 710.1.HF6: the tape cutter info was missing in the maintenance menu.
D1-147189601
A tray could be loaded into WPC although the station recognized it as too
high later.

Station Software 711.1 (R18-1) / Version Description 05/2018 Edition
30
D1-147192301 The grouping of MTC/WPC components did not work.
D1-147324601
The firmware download onto a new WPC6 failed 2 times with a controller
error 30016.
D1-147775001
Sporadically, the station software stopped during placement with error
message
30016 Unhandled exception error
.
D1-148003112
eSW: the board was transported from the intermediate section into placement
area 2 but did not get clamped.
D17647-21801 High reject rate for special component (spacer).
D17928-22501
The image was displayed distorted when the "correct position" function was
used.
D17933-45306
The machine tried to recognize an incorrect tray fiducial repeatedly without
stopping.
D18093-25513 The tray data in the generated traceability files was incorrect.
D18093-25601
Download without empty machine: it was not possible to verify components
after a program download while production was running. All feeders were
locked.
D18405-2201
The station software hung up when the pickup position was checked after a
pickup error.
Table 9-3: Corrected errors station software version 710.1 SP1
710.1 Patch 6
Error No.
Error description
D1-145731801 15µm vacuum tools could not be measured.
D1-145333801
Table 1: An error occurred while reading embedded software data from the
subsystem.
D1-145861401
Error message "32507 Product change: Finishing previous product prior to
setup change" and no more boards got into the machine.
D1-145863109
The calculation of the remaining time until the package is used up was not
correct.
D1-146194301
The calculation of the remaining time was not correct when synchronous dual
conveyor was configured.
D18433-301 Production stopped due to an unspecific hardware error of the axis.
D1-138937301
Placement offset of a heavy component because the gantry moved with full
speed during gantry repression.
D1-145522401 The WPC pickup process did not always start at the first pocket.
D18403-209 eSW: The X-axis motor hit the buffer mount of the X axis.
D1-146221801 The WPC pickup position was not calculated correctly.
Table 9-4: Corrected errors station software version 710.1 Patch 6

Station Software 711.1 (R18-1) / Version Description 05/2018 Edition
31
710.1 Patch 5
Error No.
Error description
D1-140785106
eSW: boards without board barcode required manual confirmation when they
were transported into the next machine.
D1-142933001
eSW: PCB-A interface: the board did not drive into the machine when the
acceleration was too small (< 1400 mm/s²).
D1-143801301
When the acceleration values were taught at the station, the x-axis values
were not transferred.
D1-145171201 Although the panel was marked with an ink spot, it got assembled.
D1-145202821 Restoring the conveyor configuration after mapping did not work.
D1-145232501 The software hung up after having sent a job.
D1-145282601
When conveyor lane 2 was calibrated, the conveyor control stopped with error
message
ISS software is not responding
.
D1-145398946
eSW: although there was no board in the output area, the machine displayed
one and could not continue production.
D1-145422501
eSW: the board moved directly from PA2 to the next machine; it did not stop
in the output area if the next machine was blocked.
D1-145571791
D1-145633801
D1-145658101
There was an IPC communication error when you pressed the display,
check and setup feeders button on the station software and the view
changed to
deactivated feeders
.
D1-145603609
D1-143839501
Sporadically the station software stopped during placement with error
message
30016 Unhandled exception error
.
D1-145691301 During production, gantry 2 stopped without any warning or error on the GUI.
D18294-3901 eSW: error message 35200 Board has not arrived in specified section.
Table 9-5: Corrected errors station software version 710.1 Patch 5
710.1 Patch 4
Error No.
Error description
D1-135126702 Head Verification: DP rotation and segment offset up tests were not possible.
D1-135126745
The Z axis movement and vacuum calibration tests failed but the machine
was ok.
D1-136288601 The board was transported into the input area and was not moved further.
D1-137766301 The teaching of acceleration values failed and component got lost.
D1-138967301 The use of an alternative LDU on the same table was not supported.
D1-139882801
The WPC tray was still moving when the head was ready for pick up. This
slowed down the machine.
D1-140734101
Head cycle count did not match between SIPLACE Pro optimized results and
actual machine run.
D1-141055501
Error message 35026 Pickup location is not ready although the
feeder seemed to be ready.
D1-141676501
Pocket recognition after a manual teaching process added the new position
value to the formerly detected one.