M20_Ope_E.pdf - 第452页

offset. X:%d1 Y:%d2 Alarm:%d3 T:%d4 Alarm:%d8 range. Check the parameter setting. 1479 Dispense Nozzle Offset OK Head%c1 Angle:%d2 X:%d3 Y:%d4 T:%d5 The number of adjustments:%d8 1440 Unclamp MX-ST2. Reached the limit of…

100%1 / 518
%d8 Step:%d5 Offset:%d6
pressure.
1439 Clamp MX-ST2. Clamp MX-ST2.
Check ANC shutter and missetting of nozzle. Contact
1385 ANC scanning error
us for ANC scanning error.
1386 MX-40 pallet setting error Check pallet information or MX-40.
1387 MX-40 origin acquisition error Check MX-40.
1388 MX-40 shuttle contacts conveyor rail. Check conveyor rail position.
1389 Feeder cannot operate. Check feeder for misfeeding.
1390 Signal output operation error System is abnormal. Contact us.
1391
1392
PS-32A tape-peeling error %s (%d1)
PS-32A re-positioning error %s (%d1)
Check Feeder Setting or check the feeder.
Check Feeder Setting or check the feeder.
PS-32A sequence clear command control error %s
1393
(%d1)
Check Feeder Setting or check the feeder.
1394 MX-20 pallet setting error (Pallet-%d1) Check pallet information or MX-20.
1395 MX-20 origin acquisition error (Pallet-%d1) Check MX-20.
1396 MX-F20 shuttle contacts conveyor rail. Check conveyor rail position.
1397 Failed to retract MX-40 pallet Check MX-40 setting and conditions of MX-40B
1398 Failed to retract MX-20 pallet (Pallet-%d1) Check MX-20 setting and conditions of MX-20F
1399 Failed to retract %s pallet (Pallet-%d2) Check pallet information or MXR.
1400 %m
1401 %s is open.
1402 %s is pressed.
1403 Origin detection starts.
1404 Sensor of the safety guard responded.
1405 Origin has been detected.
1406 Waiting for Board arrival at %s. Waiting for Board arrival.
1407 Board starts to enter at %s. Just started Board transfer in.
1408 Board has arrived at %s. Completed Board transfer in.
1409 IN sensor detects board.
1410 Buffer sensor detects board.
1411 Arrival sensor detects board.
1412 OUT sensor detects board.
1413 Board clamp starts.
1414 Board clamp ends.
1415 Board unclamp starts.
1416 Board unclamp ends.
1417 Board is ready to be conveyed out at %s. Board is ready to be conveyed out.
1418
1419
Board starts to be conveyed out at %s.
Board has been away from %s.
Just started Board transfer out.
Completed Board transfer out.
1420
Canceled the job with the multiple-pickup cycle
halfway done.
When production is cancelled without completing
Cannot handle the multiple-pickup cycle by normal
resume procedure.
1421 postponed components, restart the production by
selecting Continue"."
Postponed components cannot be placed by selecting
Start from the selected row.""
1422 Canceled the job with components being picked up.
Remove the picked up components to resume
production.
No program step to execute. Pass the PCB through. No program step to execute due to component skip
1423
%s or etc. Check components.
1424 Waiting for Board arrival at %s. Waiting for Board arrival.
1425
1426
Board starts to enter at %s.
Board has arrived at %s.
Just started Board transfer in.
Completed Board transfer in.
1427
Pickup error %m %s-%d3 Head%c1 Nozzle No.%d2
%d7 < %d8 Step:%d5 Offset:%d6
Check status of Head, Component, and Pickup point.
1428
Pickup error (no countermeasure) %m %s-%d3
Head%c1 Nozzle No.%d2 %d7 < %d8 Step:%d5
Choke pressure error Head%c1 Nozzle No.%d2 %d7
1429
> %d8
Nozzle is choked.
1430 Feeder indexing starts.
1431 %s can be set up. Replenish components.
1432 Feeder indexing ends.
1433 %s waits to be unloaded.
1434
1435
Unloading PCB from %s starts.
Unloading PCB from %s is complete.
1436
Coplanarity measurement error %m %s-%d3 Head%c1
Nozzle No.%d2 Step:%d5 Offset:%d6
1437
On-head component is brought back (vision
inspection) %m %s-%d3 Head%c1 Nozzle:%d2
On-head component is brought back (pneumatic
Check the placement point and the nozzle for dirt.
1438 inspection) %m %s-%d3 Head%c1 Nozzle:%d2 %d7 >
Check that the nozzle is not choked. Check the air
offset. X:%d1 Y:%d2 Alarm:%d3 T:%d4 Alarm:%d8 range. Check the parameter setting.
1479
Dispense Nozzle Offset OK Head%c1 Angle:%d2 X:%d3
Y:%d4 T:%d5 The number of adjustments:%d8
1440 Unclamp MX-ST2.
Reached the limit of pickup or vision-process error
Unclamp MX-ST2.
1441 count. Feeder Skip %m %s-%d3 Head%c1 Nozzle:%d2
Step:%d5 Offset:%d6
Other feeder(s) will be used. The feeder will be
skipped from now on.
1442
Nozzle is detected on Head%c1. Does not agree with
inf. on Head-Nozzle Setup.
Nozzle change by hand is prohibited. Check if the tip
of the head is clean.
Nozzle is not detected on Head%c1. Does not agree
1443
1444
with inf. on Head-Nozzle Setup.
Nozzle change by hand is prohibited.
Specified number of PCBs have been produced. Press the Cancel switch to abort.
Failed to scan the PCB code. When a placed PCB is
1445
1446
unloaded, the mounter will pause by an error.
%m mode
The PCB code is scanned. When a placed PCB is
1447 unloaded, the program will be switched to the scanned
program.
Make settings of Dot Station Dispense Check in the
1448
1449
Dispense Check Data for Head%c1 is not found.
FL detect correction is disabled.
dispense check program.
FL detect correction is disabled in the user
1450
Both the FL detect correction and the vision
correction are enabled.
Select either FL detect correction or vision
correction.
Image processing result %m %s%c8 Head%c1 X:%d2
1451
Y:%d3 T:%d4 (%d5,%d6,%d7)
Component image is taken by camera.
1452 Setup of %s starts.
1453
1454
Setup of %s ends.
%s #%d1 component is set. (Components:%d2)
Updated the initial pickup point for %s [ #%d1 (P%d2#-
1455
%d3 pallet) ].
1456 %s CFB is locked.
1457 %s CFB is released.
1458
1459
%s pallet is returned.
The system switched to the %s mode.
1460
AMF Fiducial. Code:%d1 Group:%d2 X;%d3 Y:%d4 T:%d5
( %d6 %d7) %m
AMF Placement Head%d1 Angle:%d2 X:%d3 Y:%d4 T:%d5
1461
1462
(%d6 %d7 %d8) %m
Halt of head movement during PCB arrival wait %s
1463
Resumption of head movement on completion of PCB
arrival. PCB arrival wait time: %d1.%d4 seconds %s
1464
Area detection event error.(%d1 %d2:%d5 %d3->%d4
[%d8])
Obtain log data by clicking the <LOG> button and
contact us.
1465
Axis status mismatch.(X:%d1 %d2->%d3 Y:%d4 %d5-
>%d6 [%d8])
Obtain log data by clicking the <LOG> button and
contact us.
1466 The sensor detected the fluid shortage on Head%c1. Replenish the head with fluid in good time.
1467 Area interlock has been detected.
Obtain log data by clicking the <LOG> button and
contact us.
1468
1469
1470
Switched to MX-40 upper stocker.
Switched to MX-40 lower stocker.
Timeout in temperature control for Head%c1 Check the temperature controller.
1471
Dispensing was started without the set temperature
being reached for Head%c1. Target:%v2deg C Check the temperature controller.
1472
Current:%v3deg C
Halt of Head%c1 movement for awaiting completion of
temperature control
1473
Short of OK counts for Head%s. OK count:%p2
Average ratio:%d3% Tolerance:%d4%-%d5%
Pressure:%v6Mpa Correction coefficient:%v1 %m
Number of retrials exceeded the Max Check Count
OK count < Min OK Count. Check the nozzle, syringe,
parameters.
1474
for Head%s. OK count:%p2 Average ratio:%d3% Number of retrials exceeded the specified Max Check
Tolerance:%d4%-%d5% Pressure:%v6Mpa Correction
coefficient:%v1 %m
Count. Check the nozzle, syringe, parameters.
1475
1476
Retry/Skip is not specified. Specify whether to retry or skip.
Measure DP %s( F:%d1 X:%d2 Y:%d3 AR:%d4 LS:%d5
1477
SS:%d6 SD:%d7 T:%d8 %m )
Dispense Nozzle Offset Adjustment Head%c1
1478
Angle:%d2 X:%d3->%d4 Y:%d5->%d6 T:%d7->%d8
Error in automatic acquisition of dispense nozzle Coordinates correction values exceeded the allowable
1531 %s Hook unlock sensor ON. (Pallet-%d2) Check conditions of MXR
1532 %s Hook unlock sensor OFF. (Pallet-%d2) Check conditions of MXR
1533 %s Stocker area sensor detected a pallet. Check conditions of MXR
1480
Measure DP %s( F:%d1 X:%d2 Y:%d3 AR:%d4 LS:%d5
1481
SS:%d6 SD:%d7 T:%d8 %m )
The component %m" in step No.%d1 for repeat offset
Remain Check:%d4)"
1482
step No.%d2 will be skipped. (Head%c3
The component %m" will be skipped from the step
No.%d1 for repeat offset step No.%d2. (Head%c3)"
The component exhaustion process for %m" will be
1483 postponed from the step No.%d1 for repeat offset
step No.%d2."
1484 Paused for component exhaustion. Replenish the feeder with components to restart.
1485
Production was started with the Postpone
Component Exhaustion Process" function disabled."
To enable the Postpone Component Exhaustion
Process" function
1486
1487
Out of components (%m).
The component %m" in step No.%d1 for repeat offset
Refill the components.
1488
step No.%d2 will be postponed."
Buffer stopper error
Actuate buffer stopper in manual menu
1489
Changed to safety stop" state because %s was
(Actuator/LoadBoard).
To resume production run, close the cover and press
opened." the Servo switch.
1490
Switched to %s mode and changed to safety stop"
state."
To resume production run, close the cover and press
the Servo switch.
1491
1492
Switched to %s mode.
Switched to %s mode and changed to safety stop" To resume production run, close the cover and press
state." the Servo switch.
1493
Coordinates have been lost due to trouble in return-
to-coordinate process.
Take origin again.
1494 %c1 switch cannot be activated because %s is open. Close the cover.
1495
Job run cannot be performed because the machine is
Press the Servo switch.
in the safety stop" state."
1497
1500
%m
%s Pallet exists on hook. (Pallet-%d2)
Message
Check MXR setting
1501
1502
%s No pallet on hook. (Pallet-%d2)
%s Pallet exists on hook whereas pallet not
Check MXR setting
Check MXR setting
programmed. (Pallet-%d2)
1503
%s No pallet on hook whereas pallet programmed.
Check MXR setting
1504
(Pallet-%d2)
%s Pallet exists in stocker. Check MXR setting
1505
1506
%s No pallet in stocker. (Pallet-%d2)
%s Pallet exists in stocker whereas pallet not
Check MXR setting
Check MXR setting
programmed. (Pallet-%d2)
1507
%s No pallet in stocker whereas pallet programmed.
Check MXR setting
(Pallet-%d2)
1508 %s Pallet No. Failure in Stocker. (Pallet-%d2) Check MXR setting
1509 %s Timeout for door lock. (Pallet-%d2) Check conditions of MXR
1510 %s Timeout for door unlock. (Pallet-%d2) Check conditions of MXR
1511 %s Timeout for hook lock. (Pallet-%d2) Check conditions of MXR
1512 %s Timeout for hook unlock. (Pallet-%d2) Check conditions of MXR
1513 %s Timeout for pallet bar open. (Pallet-%d2) Check conditions of MXR
1514 %s Timeout for pallet bar close. (Pallet-%d2) Check conditions of MXR
1515 %s Timeout for pallet side clamp ON. (Pallet-%d2) Check conditions of MXR
1516 %s Timeout for pallet side clamp OFF. (Pallet-%d2) Check conditions of MXR
1517 %s Timeout for pallet rear clamp ON. (Pallet-%d2) Check conditions of MXR
1518
1519
%s Timeout for pallet rear clamp OFF. (Pallet-%d2)
%s Timeout in Elevator Movement. (Pallet-%d2)
Check conditions of MXR
Check conditions of MXR
1520 %s Timeout in Hook Movement. (Pallet-%d2) Check conditions of MXR
1521
%s Timeout for Elevator Returning to Origin. (Pallet-
Check conditions of MXR
%d2)
1522 %s Timeout for Hook Returning to Origin. (Pallet-%d2) Check conditions of MXR
1523 %s Pallet advance end sensor ON. (Pallet-%d2) Check conditions of MXR
1524 %s Pallet advance end sensor OFF. (Pallet-%d2) Check conditions of MXR
1525 %s Pallet bar open sensor ON (Pallet-%d2) Check conditions of MXR
1526 %s Pallet bar open sensor OFF (Pallet-%d2) Check conditions of MXR
1527 %s Pallet bar close sensor ON (Pallet-%d2) Check conditions of MXR
1528 %s Pallet bar close sensor OFF (Pallet-%d2) Check conditions of MXR
1529 %s Hook lock sensor ON. (Pallet-%d2) Check conditions of MXR
1530 %s Hook lock sensor OFF. (Pallet-%d2) Check conditions of MXR