M20_Ope_E.pdf - 第469页
3107 Failed to image the pickup point. Row:%d1 Offset:%d2 image data. 3108 Extra time was needed to start stable Laser check. %d1msec 3109 IC component feeding device is out of components or a malfunction occurred in the…

3075
Pallet information of %s and pallet positions in stocker
are not match. The machine recovered automatically.
Check pallet positions in stocker.
3076
Head stops while waiting for completion of CTF/FTF
tray setup
3041
3042
The CTF stopped. An error occurred on the other
than the CTF while the CTF was operating.
Check the CTF.
Feeder type set at %s-%d1 and %m in pickup data do Check that feeder type input in pickup data and the
3043
not match.
Failed to perform CFB correction.
feeder type set at the specified position are the
Check that correction marks are clean.
3044
%c4 does not reach the target coordinates.
(Head%c6%s Target %d1 Pushdown Stroke %d5
3045
Feedback %d2 Tolerance %d3 %m)
Fixed nozzle is specified to Head%d1 that handles the
Cancel the fixed nozzle setting.
3046
manipulator.
Head cannot travel in XY directions because of Z axis
Check Z axis status.
error.
3047
%d2mm component pitch is not available for the
feeder %m set at %s-%d1.
Select available component pitch.
3048 Electropneumatic regulator error
Check the electropneumatic regulator and the
communication path.
3049
3050
An error occurred while dispensing.
DotStation is not registered in Pickup Data.
Contact us.
Create DotStation row in Pickup Data and specify
Station No.
3051
3052
DotStation is not mounted at %s-%d1. Check DotStation.
Dispense head cannot exchange nozzles. Dispense head tried to exchange nozzles.
Head%s Dispense Correction OK count:%p2 Average
3053 ratio:%d3% Tolerance:%d4%-%d5% Pressure:%v6Mpa
Correction coefficient:%v1 Retry Count:%d7 %m
Executing Dispense Correction
3054
Dispense head%s height check error, Difference:
%v1mm Tolerance:%v2mm Laser check:
3055
%v3mm,%v4mm Encoder check: %v5mm,%v6mm
Feeder pitch error. %s-%d1 %m (Skipped pickup data To restart, undo the un-skipped rows or press Reset
3056
of F3 cannot be reset during a job.)
Temperature reached target temperature. For your
safety, the machine will pause.
switch.
Clear the alarm. Then restart the job.
3057
Height offset of DP head%s is out of tolerance.
Offset:%v1mm, Tolerance:%v2 to %v3mm
Check that dispense nozzle is attached securely.
3058
Dispense recheck of Head%s OK count:%p2 Average
ratio:%d3% Allowable range:%d4%-%d5% Dispense check retry will be performed.
3059
Pressure:%v6Mpa Correction coefficient:%v1 Retry
PCB warp check point exists outside of PCB. %s
Check point %d1 Limit %d2
Check that no placement data exists outside of PCB
area.
3060
Motor alarm is detected on %c2%s when Ready switch
is turned On. (Alarm code %d1 %e)
3061
By PCB height check, measured height or calculated
correction height exceeds the tolerance. Step:%d1, Check that there is no obstacle or dirt on PCB.
3062
Offset:%d2
Failed to execute PCB warp check. Coordinates X: Check that there is no through-hole or notch at
3063
%v1mm, Y: %v2mm
Laser check results are unstable. Coordinates X:
check points.
Check that there is no obstacle or dirt on PCB.
3064
%v1mm, Y: %v2mm
Comp Pitch of Feeder %m at %s-%d1 is changed from
3065
%d2mm to %d3mm.
Auto PCB warp check is available up to 10000 rows
Select Manual.
including repeat task rows.
3066
Feeder setup is verified. Feeder setup count %d1,
Feeder count in Pickup data %d2
3067
Feeder setup count %d1, Feeder count in Pickup data
%d2
3068 Server access timeout is detected. %s-%d1 ID:%d2- Check the connection of the server.
3069
F3 feeder information %s-%d1 %m, Serial No.%d3,
Component pitch %d4mm, Internal error code %d7 %e
3070
All push-up pins are on the holder. (Registered: %d1,
3071
3072
On Holder: %d2)
%s was changed to the setup state.
%s was changed to the components supply state.
3073
3074
%s stocker cover is open.
%s servo is off.

3107 Failed to image the pickup point. Row:%d1 Offset:%d2
image data.
3108
Extra time was needed to start stable Laser check.
%d1msec
3109
IC component feeding device is out of components or
a malfunction occurred in the device.
Please check IC component feeding device.
3077
Head will start traveling after completion of CTF/FTF
tray setup
3078
The component cannot be put back to the tray for
reuse because %s is in Nonstop tray setup mode. To
Press Setup switch to allow CTF/FTF to supply
components.
3079
cancel the mode, press Setup switch.
Laser calibration is interrupted.
3080
3081
Laser calibration error occurred.
Laser tool horizontal error
Tool is not horizontally assembled. Check the
3082 Laser height scale error
assembled condition.
Re-adjust the laser head assembling. Then re-
3083 Laser height check range error
execute auto calibration.
Re-adjust the laser head assembling. Then re-
3084 Laser Z offset check error
execute auto calibration.
Re-adjust the laser head assembling. Then re-
3085
3086
Laser XY offset check error
Laser immeasurable check error
execute auto calibration.
Re-execute provisional adjustment of XY offset. Then
execute auto calibration.
Make sure no dirt or obstacles are at laser transmit
part. Then re-execute auto calibration.
3087
Cannot set the feeder at the pickup station because
the feeder pickup point height exceeds the height of
limit range. %s-%d1 %m %v2mm < %v3mm
To set the feeder at a feeder station, 'ST-F1 to 13 on
M10', or 'ST-FR24 to 36 or ST-FL1 to 13 on M20',
feeder pickup point height, sum of Pickup 'Z offset' +
Feeder 'Feed height' + Package 'Height'" must be
5mm or less. (Minus Z offset is not added.)"
To set the feeder at a pickup station, 'ST-F1 to 13 on
Cannot set the feeder because Device Max Height of
M10', or 'ST-FR24 to 36 or ST-FL1 to 13 on M20',
3088 the feeder exceeds the height of limit range. %s-%d1
sum of the device max height and the feeder height
3089
%m %v2mm < %v4mm
%s communication error
must be 5mm or less.
3090
3091
%s servo error
READY %s X,%d1,Y,%d2,Z,%d3,%d4,%d5,%d6,%d7,%d8
3092 READY %s R,%d3,%d4,%d5,%d6,%d7,%d8
Angle of Dispense nozzle exceeds tolerance. Head%d1
3093
Shift: %v2 Tolerance: %v3
Refix the Dispense nozzle.
Never set a feeder during production to prevent a
3094 A feeder is set at %s-%d1 during production.
head crash.
A feeder is removed from %s-%d1 during production. Never remove a feeder during production to prevent a
3095
(The feed button of F1 or F2 feeder was pressed.) head crash.
Comp Pitch of Feeder %m at %s-%d1 is changed from
3096
%d2mm to Default.
Comp Pitch of Feeder %m at %s-%d1 is changed from
3097
3098
Default to %d3mm.
Comp Pitch of Feeder %m at %s-%d1 is selected to
Default.
Comp Pitch of Feeder %m at %s-%d1 is selected to
3099
%d2mm.
Image process is resulted in NG because failed to
3100 acquire the acceleration and/or the speed of image
capture. %m Head%c1
3101 Failed to check Dispense nozzle length. Head%d1
The offset value in the dispense data exceeds
Check that Dispense nozzle is attached properly.
Correct the offset value in Dispense Data to be within
3102
DotStation area.
Component is placed out of PCB %m Head%c1
DotStation area.
Check PCB size, placement point, component data,
3103
Row:%d5 Offset:%d6
Placement error reaches limit count. %m Head%c1
selected nozzle, and image data.
Check PCB size, placement point, component data,
3104
Row:%d5 Offset:%d6 selected nozzle, and image data.
Shortage of disk space or cannot connect a network
3105 Cannot save a log file.
drive.
Cannot drive because version of the right and the left
3106
servo amplifiers differ. Y1-AMP:%X1 Y2-AMP:%X2
Use X and Y Servo amplifiers of version E4.001.
Check the Pickup point status and the Component

3118
The conveyor width was changed after Push up pins
were located. Located %v1mm, Current %v2mm,
Tolerance +/-%v3mm
Collect the Pushup Pins manually.
3119
Push-up pin location is the same as the last time.
The process has been skipped.
Diameter of each dispensing point of multi-nozzles
cannot be compensated to the target diameter. One
3110 dispensing diameter exceeds the maximum acceptable
diameter and another dispensing diameter falls the
Please check the target diameter of each dispensing
point.
3111
minimum acceptable diameter.
Height Check NG %m %d2th row Result:%v3
Tolerance:%v4 Head%c1 Row No.:%d5 Repeat
Check the component configuration and position.
3112
Height Check NG reached retry limit %m Head%c1
Row No.:%d5 Repeat Offset:%d6
Check the component configuration and position.
3113
The PCB on the conveyor may not be reloaded.
At the start of production, the PCB was detected at
an improper position to reload. Remove the PCB and
Remove the PCB.
Adjusted offset values of Dispense Nozzle Head:%c1
Restart the production.
3114
Angle:%d2 X:%d3 Y:%d4 T:%d5
Height of the Quick Clamp is not proper. Checked %v1 Check the Quick Clamp motion. Check that no
3115
3116
Set Height %v2
Differences of check results of Laser1 and Laser2
exceed the tolerance. 1st:%v1 2nd:%v2 Tolerance:%v3
obstacles between the Quick Clamp and the
Check the lasers installation status.
3117
The Reject Conveyor %c2-%d3 in Pickup Data No. %d6
is full or not installed.
Remove components and press the RESET button. Or
install the Reject Conveyor at the proper station.