FUJI错误代码查询.pdf - 第214页
MTU is of the type where air is supplied from the IP machine, check that the air pressure sensor is not installed. In this case also check that the inputs for the air pressure sensor are short circuited. ----------------…
Used by: MTU3,MTU4,MTU5
Cause: The X axis is outside the software limit set in the MTU Proper data.
Remedy: Move the X axis to within the software limit and check that the values set in Proper data agree.
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Code: 1108104A
Display: Software limit: Check Y
Used by: MTU3,MTU4,MTU5
Cause: The Y axis is outside the software limit set in the MTU Proper data.
Remedy: Move the Y axis to within the software limit and check that the values set in Proper data agree.
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Code: 1108104B
Display: Software limit: Check Z
Used by: MTU3,MTU4,MTU5
Cause: The Z axis is outside the software limit set in the MTU Proper data.
Remedy: Move the Z axis to within the software limit and check that the values set in Proper data agree.
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Code: 1108104C
Display: Software limit: Check T
Used by: MTU4
Cause: The T axis is outside the software limit set in the MTU Proper data.
Remedy: Move the T axis to within the software limit and check that the values set in Proper data agree.
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Code: 11081060
Display: 11081060
Used by: MTU3,MTU4,MTU5
Cause: The sub-robot moved into the interference range defined by the MTU Proper data.
Remedy: Check the MTU Proper data (tray origin point, interlock etc).
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Code: 11081061
Display: REDUCE SY Sensor Went Off During T Axis Movement
Used by: MTU4
Cause: The Y axis speed reduction sensor was off while the T axis was moving.
Remedy: Check the Y axis speed reduction sensor and the dog.
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Code: 11081062
Display: TRAY SPACE OK Sensor Went Off During SY Axis Movement
Used by: MTU4
Cause: The T axis robot safety sensor was off while the SY axis was moving.
Remedy: Check the T axis robot safety sensor and the dog on the tray which caused the error.
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Code: 11081063
Display: SZ READY Sensor Went Off During SY Axis Movement
Used by: MTU4
Cause: The Z axis interlock sensor was off while the Y axis was moving.
Remedy: Check the Z axis interlock sensor and the dog.
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Code: 11081070
Display: Air Pressure Alarm
Used by: MTU3,MTU4,MTU5
Cause: The air pressure sensor detected a drop in the air pressure.
Remedy: Check that air is being supplied and that the air pressure is not falling. Furthermore, if the
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MTU is of the type where air is supplied from the IP machine, check that the air pressure sensor is not
installed. In this case also check that the inputs for the air pressure sensor are short circuited.
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Code: 11081080
Display: MTU not Zero set Properly
Used by: MTU4
Cause: An error occurred during zero setting.
Remedy: Check the T axis speed reduction sensor and the robot safety sensor.
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Code: 11081081
Display: Part Carrier: Zero Setting Failed
Used by: MTU4
Cause: When the carrier retracted, the retract end sensor did not come on within the prescribed time.
Remedy: Adjust the carrier retract end sensor.
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Code: 11081083
Display: Y Axis Deceleration Sensor is Not ON at Nozzle change
Used by: MTU4
Cause: The Y axis speed reduction sensor was not on when the nozzle was changed at zero setting.
Remedy: Adjust the Y axis speed reduction sensor and the dog.
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Code: 11081084
Display: Z Axis Deceleration Sensor is Not ON at Nozzle change
Used by: MTU4
Cause: The Z axis speed reduction sensor was not on when the nozzle was changed at zero setting.
Remedy: Adjust the Z axis speed reduction sensor and the dog.
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Code: 11081085
Display: Nozzle Changer is Not at Retract Limit Position
Used by: MTU4
Cause: The nozzle changer retract sensor was not on when the nozzle was changed at zero setting.
Remedy: Adjust the nozzle changer retract and advance sensors.
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Code: 11081086
Display: Nozzle Pos. Sensor Error
Used by: MTU4
Cause: When the nozzle rotated during zero setting, the nozzle position sensors did not turn on at the
correct positions.
Remedy: Check the nozzle position sensors, the dogs and the nozzle changer.
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Code: 11081087
Display: Tray Set Off at Zero Set
Used by: MTU4
Cause: During zero setting the tray set sensor was activated.
Remedy: Check that the trays are correctly set in place and that the tray door is closed.
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Code: 11081088
Display: Y Axis Deceleration Sensor and Tray Space Chk Sensor is Not ON at Zero Set
Used by: MTU4
Cause: During zero setting neither the Y axis speed reduction sensor nor the robot safety sensor was on.
Remedy: After manually turning on the Y axis speed reduction sensor, inch the T axis and turn on the
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robot safety sensor.
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Code: 11081090
Display: TRAY SET OFF
Used by: MTU4
Cause: The tray set check sensor was off while the T axis was moving (other than during inching).
Remedy: Check that the tray plate is correctly positioned.
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Code: 11081091
Display: Tray positioning sensor is not on.
Used by: MTU4
Details: The tray positioning sensor is not on.
Cause:
Remedy: Adjust the robot safety sensor.
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Code: 11081092
Display: Tray positioning sensor is not off.
Used by: MTU4
Details: The tray positioning sensor is not off.
Cause:
Remedy: Adjust the robot safety sensor.
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Code: 110810A0
Display: Software limit: Check +X
Used by:
Cause: During automatic operation, the X axis moved to a position (in the plus direction) outside the
software limit set in Proper data.
Remedy: Check the MTU Proper data and the items in part data related to movement, and set correct
data.
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Code: 110810A1
Display: Software limit: Check -X
Used by: MTU3,MTU4,MTU5
Cause: During automatic operation, the X axis moved to a position (in the minus direction) outside the
software limit set in Proper data.
Remedy: Check the MTU Proper data and the items in part data related to movement, and set correct
data.
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Code: 110810A2
Display: Software limit: Check +Y
Used by: MTU3,MTU4,MTU5
Cause: During automatic operation, the Y axis moved to a position (in the plus direction) outside the
software limit set in Proper data.
Remedy: Check the MTU Proper data and the items in part data related to movement, and set correct
data.
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Code: 110810A3
Display: Software limit: Check -Y
Used by: MTU3,MTU4,MTU5
Cause: During automatic operation, the Y axis moved to a position (in the minus direction) outside the
software limit set in Proper data.
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