FUJI错误代码查询.pdf - 第219页

Code: 11082310 Display: Pickup Recovery Counter Limit Reached Used by: MTU3,MTU4,MTU5 Cause: The sub-nozzle was unable to pick up a part in the tray and therefore reattempted to pick up the part the specified number of t…

100%1 / 5282
------------------------------
Code: 11082220
Display: Servo Power is ON
Used by: MTU3,MTU4,MTU5
Cause: While the servo power was on at the MTU, the IP machine issued a command for when the servo
power is off.
Remedy: Reset the error at the IP machine. If the error occurs repeatedly, contact Fuji.
------------------------------
Code: 11082221
Display: Servo Power is OFF
Used by: MTU3,MTU4,MTU5
Cause: While the servo power was off at the MTU, the IP machine issued a command for when the servo
power is on.
Remedy: Reset the error at the IP machine. If the error occurs repeatedly, contact Fuji.
------------------------------
Code: 11082230
Display: Operation Mode is set to OPERATE
Used by: MTU3,MTU4,MTU5
Cause: While the MTU was operating, commands for use when the MTU is stopped were issued by the IP
machine.
Remedy: Reset the error at the IP machine. If the error occurs repeatedly, contact Fuji.
------------------------------
Code: 11082231
Display: Operation Mode is set to Stop
Used by: MTU3,MTU4,MTU5
Cause: While the MTU was operating, commands for use when the MTU is stopped were issued by the IP
machine.
Remedy: Reset the error at the IP machine. If the error occurs repeatedly, contact Fuji.
------------------------------
Code: 11082240
Display: Remove empty tray
Used by: MTU4
Cause: An emergency stop occurred after the last part in the tray had been picked up and before the tray
was ejected. Because the emergency stop occurred during the tray eject cycle, the MTU is unsure of the
condition of the tray. Therefore it is necessary for the operator to check the tray and remove it.
Remedy: Manually remove the empty tray.
------------------------------
Code: 11082250
Display: Operation Impossible MTU Operation Panel in Use
Used by: MTU3,MTU4,MTU5
Cause: Operation was being performed at the MTU terminal when AUTO, STEP or another command was
executed at the IP machine.
Remedy: At the MTU terminal us
------------------------------
Code: 110822EE
Display: Command can not be Executed due to Alarm
Used by: MTU3,MTU4,MTU5
Cause: While the MTU was in an error condition, an instruction to start production was issued by the IP
machine.
Remedy: Reset the error at the IP machine. If the error occurs repeatedly, contact Fuji.
------------------------------
第 218 页
Code: 11082310
Display: Pickup Recovery Counter Limit Reached
Used by: MTU3,MTU4,MTU5
Cause: The sub-nozzle was unable to pick up a part in the tray and therefore reattempted to pick up the
part the specified number of times, again without success.
Remedy: Check that the tray is correctly positioned and that the parts with in the tray are correctly
positioned. Also check that correct data has been specified in part data.
------------------------------
Code: 11082330
Display: Nozzle Selection Error
Used by: MTU4
Cause: A nozzle which cannot be used on the MTU was specified.
Remedy: Reset the error at the IP machine. If the error occurs repeatedly, contact Fuji.
------------------------------
Code: 11082331
Display: Y Axis Deceleration Sensor is Not ON at Nozzle change
Used by: MTU4
Cause: When an attempt was made to change a nozzle, the Y axis speed reduction sensor was not on.
Remedy: Adjust the Y axis speed reduction sensor and the dog. In addition check that suitable data has
been entered for the MTU Proper data item Carrier_Position_SY.
------------------------------
Code: 11082332
Display: Z Axis Deceleration Sensor is Not ON at Nozzle change
Used by: MTU4
Cause: When an attempt was made to change a nozzle, the Z axis speed reduction sensor was not on.
Remedy: Adjust the Z axis speed reduction sensor and the dog. In addition check that suitable data has
been entered for the MTU Proper data item Parts_Pos_Zt0.
------------------------------
Code: 11082333
Display: Nozzle Pos. Sensor Error
Used by: MTU4
Cause: When the nozzle rotated, the nozzle position sensors did not turn on at the correct positions.
Remedy: Check the nozzle position sensors and the dogs.
------------------------------
Code: 11082334
Display: Nozzle Changer is Not at Retract Limit Position
Used by: MTU4
Cause: During nozzle change, the nozzle changer retract end sensor was not on.
Remedy: Adjust the nozzle changer retract end and advance end sensors.
------------------------------
Code: 11082335
Display: Nozzle Changer is Not at Forward Limit Position
Used by: MTU4
Cause: During nozzle change, the nozzle changer advance end sensor was not on.
Remedy: Adjust the nozzle changer advance end sensor and the dog.
------------------------------
Code: 11082340
Display: Parts Dropped From Sub-Nzl (Remove Part)
Used by: MTU4
Cause: A part picked up by the sub-nozzle was dropped while the Z axis was ascending.
Remedy: Remove the part which was dropped.
第 219 页
------------------------------
Code: 11082341
Display: Illegal Part is Sub Nozzle (Remove Part)
Used by: MTU4
Cause: This error occurs when the machine judges that there is an undefined part on the sub-nozzle (for
example, the operator may have intentionally placed a part on the sub-nozzle).
Remedy: If there is a part on the sub-nozzle, remove it. Furthermore, check the part detection sensor.
------------------------------
Code: 11082350
Display: Part Not Been Transferred From Sob-nozzle to Carrier
Used by: MTU4
Cause: A picked part was dropped while the Z axis was moving from its ascent position to the position
where the part is placed on the carrier.
Remedy: Remove the part which was dropped
------------------------------
Code: 11082351
Display: Part Dropped During Carrier Movement (Remove Part)
Used by: MTU4
Cause: The part being moved into the machine by the carrier fell off the carrier.
Remedy: Remove the part which fell.
------------------------------
Code: 11082352
Display: Part Pusher Up Limit Sensor is Not ON
Used by: MTU4
Cause: When the clamp installed at the carrier 2nd position was raised, the up sensor did not come on.
Remedy: Check that air is being supplied and that the clamp mechanism and up sensor are functioning
normally.
------------------------------
Code: 11082353
Display: Part Pusher Down Limit Sensor is Not ON
Used by: MTU4
Cause: When the clamp installed at the carrier 2nd position was lowered, the down sensor did not come
on.
Remedy: Check that air is being supplied and that the clamp mechanism and down sensor are
functioning normally.
------------------------------
Code: 11082354
Display: Illegal Part is On Carrier (Remove Parts On Carrier)
Used by: MTU4
Cause: This error occurs when the machine judges that there is an undefined part on the carrier (for
example, the operator may have intentionally placed a part on the carrier).
Remedy: If there is a part on the carrier, remove it. Furthermore, check the part detection sensors at the
1st and 2nd positions.
------------------------------
Code: 11082355
Display: Carrier No.2 Pos. is In Part Data In Spite of No Part Pusher
Used by: MTU4
Cause: This error occurs if the 5th bit in the MTU4 Proper data item Machine_status is set to 0 (
indicating that the part clamp is not fitted), but in part data the 2nd position is specified.
Remedy: Check that there are no parts for which Carrier_select in part datais set to 1 (the 2nd position
setting) and that even if the parts clamp is installed, the 5th bit from the right in Machine_status is set to
第 220 页